电动汽车电池包搅拌摩擦焊缝泄漏故障分析

Leakage Failure Analysis of Friction Stir Welds in an Electric Vehicle Battery Pack

  • 摘要: 针对某电动汽车电池包下托盘在批量生产中出现的搅拌摩擦焊(Friction Stir Welding,FSW)焊缝泄漏故障,开展系统的失效分析,定位缺陷并阐明其产生机理,进而提出有效的工艺优化方案。对泄漏电池包进行气密性检测以复现并定位故障点,通过宏观观察与金相分析(OM)对缺陷形貌进行表征,并结合焊接工艺过程分析缺陷成因。结果表明:泄漏根本原因确定为FSW过程中因搅拌针严重偏置导致的“冷焊”型未焊合缺陷,该缺陷形似裂纹,构成贯穿泄漏通道。通过引入激光跟踪系统将搅拌针对中偏差控制在±0.2 mm以内,并优化工艺参数至转速1500 rpm、焊速800 mm/min,有效消除了该缺陷。精确控制搅拌针与焊缝对中性是避免此类泄漏缺陷的关键。优化后的工艺经批量验证,使焊缝泄漏率显著下降,产品合格率稳定在99.8%以上,接头平均强度达母材的73.5%,为提升电池包FSW焊缝质量与可靠性提供了有效的实践方案。

     

    Abstract: This study investigates the root cause of leakage failure in the friction stir weld (FSW) of an electric vehicle battery pack lower tray during mass production. It aims to identify the defect, clarify its formation mechanism, and propose effective process improvements.The leakage fault was reproduced and located through helium leak testing. Macro-observation and metallographic examination (OM) were employed to characterize the defect morphology, combined with an analysis of the welding process to determine the cause.The results show that the leakage was attributed to a lack-of-penetration defect, specifically a "cold weld, " caused by severe stirring pin deviation during FSW. This defect, resembling a crack, created a continuous channel for leakage. By implementing a laser tracking system to control pin alignment within ±0.2 mm and optimizing parameters to a rotation speed of 1500 rpm and a travel speed of 800 mm/min, the defect was effectively eliminated. Precise control of stirring pin alignment is critical for preventing such leakage defects. The optimized process, validated through batch production, significantly reduced the leakage rate, achieving a consistent product qualification rate above 99.8% and a joint strength reaching 73.5% of the base material. This provides an effective solution for enhancing the quality and reliability of FSW joints in battery packs.

     

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